On december 10th, 2023, we went to Burlington for a scrimmage. It was a great check-in to see how our robot will preform at a qualifier.


We discovered a few issues during this time but still managed to be placed first in the qualifying matches and made our way to finals losing 1:2 despite a broken autoload. Without our autoload we were left unable to pick up pixels and place them on the back drop. We still shot our drone and hung on the rigging along with our autonomous program. Luckily our teammate 21351 Cybotz was able to place the pixels we gave them during gameplay. We were able to coordinate and create the best out of the situation.

We have now fixed our autoload and a problem we were having of our team markers falling off during matches.